Thursday, December 12, 2019
Maya- PM-1 Hour-Stepper
So I worked on the Dog food dispenser project, and we started a print on the model we made and checked on it, but ti didn't finish since we started it late. We worked on coding the servo but it wasn't working no matter what we did, so we ended up switching to servo motors so that we can control the position and make sure that the food isn't accidentally always flowing. Now that that happened, we have to fix the models, but ti already started to print, so we are going to have a small issue testing it. Now we can move on to making the internet part of the arduino code.
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